I posted how I changed my B3200 over from the low amp Dynamo to the Kubota 40 amp Alternator. The factory, easily accessible , dip stick and tube that was set up for the Dynamo, would not work with the alternator. It interfered with the back of the longer alternator. Kubota called for a short oil dip stick that you really couldn't get to with the tractor engine side cover on.
So, I got to looking at the old dip stick and tube and thought I had nothing to lose trying to modify it. I carefully cut off the mounting bracket with a Dremel Tool and a small, thin cut off wheel. I then thought of how and where to re-route the dip stick tube. It is made from soft steel tubing so I carefully worked it, took some of the factory bends out of it and finally fit it up by the valve cover and oil fill cap. I re-bent the original mounting bracket, cut off some of the extra length, and marked it where it needed to be re-welded. That part of marking and welding was real tricky! The tube is thin and the bracket was thicker. I used my Miller Mig welder and just put two stitch welds on each side and then re-fit it. It took just a little tweak and I figured it was as good as I could get it. I carefully stitch welded the bracket to the tube being careful not to burn through the tubing. Kubota used only two little stitch welds then oven copper alloy brazed it. I cleaned it up after welding, painted it with something as close as I had to the Kubota engine gray and installed it.
So, I got to looking at the old dip stick and tube and thought I had nothing to lose trying to modify it. I carefully cut off the mounting bracket with a Dremel Tool and a small, thin cut off wheel. I then thought of how and where to re-route the dip stick tube. It is made from soft steel tubing so I carefully worked it, took some of the factory bends out of it and finally fit it up by the valve cover and oil fill cap. I re-bent the original mounting bracket, cut off some of the extra length, and marked it where it needed to be re-welded. That part of marking and welding was real tricky! The tube is thin and the bracket was thicker. I used my Miller Mig welder and just put two stitch welds on each side and then re-fit it. It took just a little tweak and I figured it was as good as I could get it. I carefully stitch welded the bracket to the tube being careful not to burn through the tubing. Kubota used only two little stitch welds then oven copper alloy brazed it. I cleaned it up after welding, painted it with something as close as I had to the Kubota engine gray and installed it.
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